PERFORMANCE REVIEW OF A LARGE-SCALE CO2-WAG ENHANCED RECOVERY PROJECT, SACROC UNIT - KELLY-SNYDER FIELD

被引:39
作者
KANE, AV
机构
来源
JOURNAL OF PETROLEUM TECHNOLOGY | 1979年 / 31卷 / 02期
关键词
D O I
10.2118/7091-PA
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
This paper reviews the production/injection performance of the CO//2-WAG project in the SACROC Unit in Kelly-Snyder Field in Texas. Premature breakthrough of CO//2 required an accelerated program to install CO//2 removal facilities. A costly zonal injection control program was conducted to maintain control of CO//2 production and to increase the WAG ratio. Measures taken to improve volumetric efficiency, produced CO//2 and water cut performance, and the volume of injected CO//2 required for each stock-tank barrel of incremental oil also are discussed.
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页码:217 / 231
页数:15
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