An extraction process to recover vanadium from low-grade vanadium-bearing titanomagnetite

被引:84
作者
Chen, Desheng [1 ,2 ]
Zhao, Hongxin [1 ,2 ]
Hu, Guoping [1 ,2 ]
Qi, Tao [1 ,2 ]
Yu, Hongdong [1 ,2 ]
Zhang, Guozhi [1 ,2 ]
Wang, Lina [1 ,2 ]
Wang, Weijing [1 ,2 ]
机构
[1] Natl Engn Lab Hydromet Cleaner Prod Technol, Beijing 100190, Peoples R China
[2] Chinese Acad Sci, Inst Proc Engn, Key Lab Green Proc & Engn, Beijing 100190, Peoples R China
基金
中国国家自然科学基金; 美国国家科学基金会;
关键词
Vanadium-bearing titanomagnetite; Extraction; Vanadium; D2EHPA/TBP; Hydrochloric acid leaching solution; SOLVENT-EXTRACTION; BAYER PROCESS; BY-PRODUCTS; IRON; D2EHPA; ACID; FE(III);
D O I
10.1016/j.jhazmat.2015.03.054
中图分类号
X [环境科学、安全科学];
学科分类号
083001 [环境科学];
摘要
An extraction process to recover vanadium from low-grade vanadium-bearing titanomagnetite was developed. In this study, a mixed solvent system of di(2-ethylhexyl) phosphate (D2EHPA) and tri-n-butyl phosphate (TBP) diluted with kerosene was used for the selective extraction of vanadium from a hydrochloric acid leaching solution that contained low vanadium concentration with high concentrations of iron and impurities of Ca, Mg, and Al. In the extraction process, the initial solution pH and the phase ratio had considerable functions in the extraction of vanadium from the hydrochloric acid leaching solution. Under optimal extraction conditions (i.e., 30-40 degrees C for 10 min, 1:3 phase ratio (O/A), 20% D2EHPA concentration (v/v), and 0-0.8 initial solution pH), 99.4% vanadium and only 4.2% iron were extracted by the three-stage counter-current extraction process. In the stripping process with H2SO4 as the stripping agent and under optimal stripping conditions (i.e., 20% H2SO4 concentration, 5:1 phase ratio (0/A), 20 min stripping time, and 40 degrees C stripping temperature), 99.6% vanadium and only 5.4% iron were stripped by the three-stage counter-current stripping process. The stripping solution contained 40.16 g/L V2O5, 0.691g/L Fe, 0.007 g/LTiO2, 0.006 g/L SiO2 and 0.247 g/L CaO. A V2O5 product with a purity of 99.12% V2O5 and only 0.026% Fe was obtained after the oxidation, precipitation, and calcination processes. The total vanadium recovered from the hydrochloric acid leaching solution was 85.5%. (C) 2015 Elsevier B.V. All rights reserved.
引用
收藏
页码:35 / 40
页数:6
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